The
Shuttles Thermal Protection System (TPS)
By
Dennis R. Jenkins
During
the original studies of lifting-reentry vehicles during the late
1950s and 1960s, there had been a great debate over the relative
merits of active cooling systems versus passive systems for the
vehicle structure. The active systems were attractiveon paperbut
nobody could quite figure out how to make them work. Therefore,
the choices were largely narrowed to either a hot-structure, like
that used on the X-15, or a more conventional structure protected
by some sort of insulation. The hot-structure approach required
the use of rare and expensive superalloys, and there was always
a great deal of doubt whether it would have worked on a vehicle
as large as the Shuttle. Generally, most contractors seemed to prefer
a fairly conventional structure made of titanium and protected by
a series of metallic shingles with a thick layer of insulation in
between the two. There was some investigation into ablative coatings,
but the unhappy X-15A-2 experience made just about everybody shy
away from this technology except as a last resort.
Things
began to change as the Lockheed Missiles and Space Company made
quick progress with the development of the ceramic reusable surface
insulation (RSI) concept. This work had begun during the late 1950s,
and by December 1960, Lockheed had applied for a patent for a reusable
insulation material made of ceramic fibers. The first use for the
material came in 1962 when Lockheed developed a 32-inch-diameter
radome for the Apollo spacecraft; it was made from a filament-wound
shell and a lightweight layer of internal insulation cast from short
silica fibers. But the Apollo design changed, and the radome never
flew.1
However,
the experience led to the development of a fibrous mat that had
a controlled porosity and microstructure called Lockheat®. The
mat was impregnated with organic fillers such as methyl methacylate
(Plexiglas) to achieve a structural quality. These composites were
not ablativethey did not char to provide protection. Instead
Lockheat evaporated, producing an outward flow of cool gas. Lockheed
investigated a number of fiberssilica, alumina, and boriaduring
the Lockheat development effort. By 1965, this had led to the development
of LI-1500, the first of what became the Shuttle tiles. This material
was 89 percent porous, had a density of 15 pounds per cubic foot,
appeared to be truly reusable, and was capable of surviving repeated
cycles to 2,500 degrees Fahrenheit. A test sample was flown on the
Air Force Pacemaker reentry test vehicle during 1968, reaching 2,300
°F with no apparent problems.2
Lockheed
decided to continue the development of the silica RSI but would
produce the material in two different densities to protect different
heating regimes9 pounds per cubic foot (designated LI-900)
and 22 pounds per cubic foot (LI-2200). The ceramic consisted of
silica fibers bound together and sintered with other silica fibers,
and then glaze-coated by a reaction-cured glass consisting of silica,
boron oxide, and silicon tetraboride. Since this mixture was not
waterproof, a silicon polymer was coated over the undersurface (i.e.,
non-glazed) side. This material was very brittle, with a low coefficient
of linear thermal expansion, and therefore Lockheed could not cover
an entire vehicle with it. Rather, the material would have to be
installed in the form of small tiles, generally 6-by-6-inch squares.
The tiles would have small gaps between them (averaging about 0.01
inch) to permit relative motion and allow for the deformation of
the metal structure under them due to thermal effects. A second
concern was the movement of the metal skin directly under an individual
tile; since a tile would still crack under this loading, engineers
decided to isolate the skin from the tile by bonding the tile to
a felt pad, then bonding the felt pad to the skin. Both of these
bonds were done with a room-temperature vulcanizing (RTV) adhesive.3
In
their Phase C response, Rockwell had proposed using mullite tiles
made from aluminum silicate instead of the Lockheed-developed tiles
because the technology was better understood and more mature. But
the mullite tiles were heavier and potentially not as durable. Given
the progress Lockheed had made subsequently, Rockwell and NASA asked
the Battelle Memorial Institute to evaluate both candidate systemsan
evaluation that the Lockheed product won. But the Lockheed material
was not appropriate for all applications. Very high-temperature
areas of the orbiterthe nose cap and wing leading edgeswould
use a reinforced carbon-carbon (RCC) material originally developed
by LTV for the Dyna-Soar program. The RCC would provide protection
above 2,700 °F, yet it would keep the aluminum structure of
the orbiter comfortably below its 350 °F maximum. Tiles were
used for the entire underside of the vehicle and for most of the
fuselage sides and vertical stabilizer. Black tiles could protect
up to 2,300 °F, while white tiles protected up to 1,200 °F.
Flexible reusable surface insulation (FRSI) protected areas not
expected to exceed 750 °F.4
Interestingly,
NASA and Rockwell originally believed that the leeward side (top)
of the vehicle would not require any thermal protection. But in
March 1975, the Air Force Flight Dynamics Laboratory conducted a
briefing for Space Shuttle engineers on the classified results of
the ASSET, PRIME, and boost-glide reentry vehicle (BGRV) programs
that indicated that leeward-side heating was a serious consideration.
The thermal environment was not particularly severe, but it easily
exceeded the 350 °F capability of the aluminum skin. FRSI blankets
were subsequently baselined for this area.
But
in the meantime, another problem had developedwith the tiles
themselves. As flight profiles were refined and aero-loads better
understood, engineers began to question whether the tiles could
survive the punishment. By mid-1979, it had become obvious that
in certain areas the tiles "did not have sufficient strength
to survive the tensile loads of a single mission." NASA immediately
began a massive search for a solution that eventually involved outside
blue-ribbon panels, government agencies, academia, and most of the
aerospace industry. As LeRoy Day recalled, . . . there [was]
a case [the tile crisis] where not enough engineering work, probably,
was done early enough in the program to understand the detailthe
mechanical propertiesof this strange material that we were
using . . . 5
The
final solution to the tile problem (at least this one) involved
strengthening the bond between the tiles and the felt strain-isolation
pads (SIP). Analysis indicated that although each individual componenta
tile, the SIP under the tile, and the two layers of adhesiveshad
satisfactory tensile strength, when combined as a system, the components
lost about 50 percent of their combined strength. This was largely
attributed to stiff spots in the SIP (caused by needling) that allowed
the system strength to decline as far as 6 psi instead of the baseline
13 psi. In October 1979, NASA decided on a densification
process that involved filling voids between fibers at the inner
moldline (the part next to the SIP pad) with a special slurry mixture
consisting of Ludox (a colloidal silica made by DuPont) and a mixture
of silica and water. Since the tiles had been waterproofed during
manufacture, the process began by applying isopropyl alcohol to
dissolve the water-proofing, then painting the back of the tile
with the Ludox. After air-drying for 24 hours, the tiles were baked
in an oven at 150 °F for two hours. After a visual and weight
check, each tile was re-waterproofed using Dow-Cornings standard
Z-6070 product (methyltrimethoxysilane). The densified layer acted
as a plate on the bottom of the tile, eliminating the
effect of the local stiff spots in the SIP, to bring the total system
strength back up to 13 psi.6
But
the installation presented its own problems. Rockwell quickly ran
out of time to install tiles while OV-102 was in PalmdaleNASA
needed to present the appearance of maintaining a schedule, and
Columbias moving to KSC was a very visible milestone.
So in March 1979, Columbia was flown from Palmdale to KSC
on the SCA, and quickly moved into the Orbiter Processing Facility
(OPF). Just over 24,000 tiles had been installed in Palmdale, with
6,000 left to go. But it now appeared that all of the tiles would
need to be removed so that they could be densified.
The
challenge became to salvage as many of the installed tiles as possible
while ensuring sufficient structural margin for a safe flight. The
approach developed to overcome this almost insurmountable challenge
was called the tile proof test. This involved the application of
a load to the installed tile in order to induce a stress over the
entire footprint equal to 125 percent of the maximum flight stress
experienced at the most critical point on the tile footprint. This
approach could potentially salvage thousands of installed tiles.7
The
device used for the proof test employed a vacuum chuck to attach
to the tile, a pneumatic cylinder to apply the load, and six pads
attached to surrounding tiles to react to the load. Since any appreciable
tile load might cause some internal fibers to break, acoustic sensors
placed in contact with the tiles were used to monitor the acoustic
emissions for any internal fiber breakage. The proof testing not
only salvaged tens of thousands of installed tiles, but also revealed
those tiles (13 percent failed the proof test) with inadequate flight
strengths. The tiles that failed would be replaced with densified
tiles.8
Two
other techniques were developed to strengthen tiles while they were
still on the vehicle. The first involved thick tilesusually
on the underside of the orbiterthat were relatively small.
As shock waves swept air over these tiles, they tended to rotate,
inducing high stresses at the SIP bonds. The solution was to install
a gap filler that prevented the tile from rotating.
However, this solution would not be very effective for small, thin
tiles, so a technique was developed where the filler bar surrounding
the SIP was bonded to the tiles. This was done by inserting a crooked
needle into the tile-to-tile gap and depositing RTV on top of the
filler bar. This significantly increased the total bonded footprint
and decreased the effects of a shock-imposed overturning moment.9
For
the next 20 months, technicians worked three shifts per day, six
days per week, testing and installing 30,759 tiles. By the time
the tiles were installed, proof-tested, often removed and reinstalled,
then re-proof-tested, the technicians averaged 1.3 tiles per man
per week. Sometimes it seemed like the workers were making no progress
at all. During June 1979, Rockwell estimated that 10,500 tiles needed
to be replaced; by January 1980, over 9,000 of these had been installed,
but the number remaining had ballooned to 13,100 as additional tiles
failed their proof tests or were otherwise damaged. By September
1980, only 4,741 tiles remained to be installed, and by Thanksgiving,
the number was below 1,000. It finally appeared that the end was
in sight.10
Between
April 1978 and January 1979, a team from the AFFDL conducted a review
of potential orbiter heating concerns and concluded that the OMS
pod might have unanticipated problems. To support the conclusion,
the Air Force ran a series of tests at the Arnold Engineering Development
Center (AEDC) between May and November 1979, and further tests were
run at the Naval Surface Weapons Center shock tunnel in May 1980.
It was discovered that the OMS pod structure would deflect considerably
more than originally anticipatedthe thin 8-by-8-inch tiles
were relatively weak under bending loads, and it was feared that
the tiles might fracture and separate from the vehicle. Since the
tiles had already been installed, a unique solution was developed
where each tile was "diced" while still attached to the
pod. This involved carefully cutting each of the 8-inch tiles into
nine equal parts. Each cut was carefully monitored to ensure that
neither the tile nor the underlying structure was damaged. The technique
proved so successful that it has subsequently been used on other
areas of the orbiter when needed.11
The
thermal protection system is subjected to numerous loadings from
the severe aerodynamic environment, including shocks and pressure
gradients. It was comparatively easy to model these loads for the
majority of the tiles because they were on flat surfaces on the
orbiter. However, many tiles adjacent to boundaries
(such as the wing leading edge or the windshield) did not have a
simple geometry and were difficult to analyze because they were
located in very complex flow fields. To better understand the problem,
NASA initiated a combination of flight and wind tunnel testing.
The flight testing was undertaken during 1980 at NASA Dryden with
a total of 60 flights by a McDonnell Douglas F-15 Eagle and a Lockheed
F-104 Starfighter. The F-15 was used to evaluate tiles from the
wing leading-edge closeout, wing glove, windshield closeout, and
vertical stabilizer leading edge; the F-104 tested tiles from the
elevon trailing edge and wing cove/elevon. The tiles were subjected
to a variety of aerodynamic load conditions, including flights up
to Mach 1.4 and dynamic pressures of 1,140 pounds per square foot.
Three wind tunnels were used for tile teststhe 16-foot tunnel
at AEDC, the 11-foot supersonic tunnel at NASA Ames, and the 8-foot
tunnel at NASA Langley. Various anomalies were uncovered that resulted
in at least some of the tiles being redesigned and retested.12
The
tiles around the windshield posed some unique problems because they
were subjected to high stagnation pressures that tried to lift the
tiles. All orbiter tiles are machined from blocks of RSI so that
the layers of silica material run in a direction generally parallel
to the skin of the orbiter. This grain orientation is a thermal
requirement to minimize the conduction of heat from the outer moldline
to the inner moldline (i.e., through the tile to the skin). However,
this grain orientation also causes a reduction in strength because
of the relatively low number of fibers that run vertically (perpendicular
to the orbiter skin)the vertical fibers are what a transfer
loads to the SIP. Because of the unusual aero-loads around the windshield,
researchers decided to machine the tiles with the grain perpendicular
to the Orbiter skin to provide twice the strength. But this ran
the risk of overheating the aluminum structure. A thermal analysis
revealed that the heavy framing around the windows acted as a large
heat sink that prevented unacceptable temperatures. Further structural
analysis, however, indicated that an adequate margin of safety was
still not achieved, so it was decided to bond the portion of the
tile that overhung the window directly to the glass (previously
it had not been bonded). This provided acceptable safety margins.13
1Tom
A. Heppenheimer, History of the Space Shuttle, Volume II: Development
of the Shuttle, 19721981, a draft manuscript for an upcoming
second volume of the official NASA shuttle history. Chapter 6 in
the 27 April 1999 version.
2History of the Space Shuttle, Volume II, chapter
6 in the 27 April 1999 version
3Richard P. Hallion and James O. Young, Space Shuttle:
Fulfillment of a Dream, Case VIII of The Hypersonic
Revolution: Case Studies in the History of Hypersonic Technology,
Volume 1, From Max Valier to Project PRIME (19241967),
Air Force Histories and Museums Program (Bolling AFB DC: U.S. Air
Force, 1998), pp. 11591160.
4Paul A. Cooper and Paul F. Holloway, The Shuttle
Tile Story, Astronautics & Aeronautics XIX, No.
1 (January 1981): 2434; Technology Influence on the Space
Shuttle Development, report 86-125C (Houston, Texas: Eagle Engineering,
Inc., 8 June 1986), pp. 6-4/5; Space Shuttle: Fulfillment of
a Dream, pp. 11591160.
5First quotation from The Shuttle Tile Story,
p. 25; Day quotation from an interview of LeRoy E. Day by John Mauer,
17 October 1983, pp. 56, in the files of the JSC History Office;
Space Shuttle: Fulfillment of a Dream, pp. 11611166.
6William C. Schneider and Glenn J. Miller, The
Challenging Scale of the Bird (Shuttle Tile Structural
Integrity), (paper presented at the Space Shuttle Technical
Conference (CR-2342) at JSC, 2830 June 1983), pp. 403413;
Space Shuttle: Fulfillment of a Dream, pp. 11651166.
7The Challenging Scale of the Bird,
pp. 403413.
8The Challenging Scale of the Bird,
pp. 403413.
9The Challenging Scale of the Bird,
pp. 410413.
10Space Shuttle: Fulfillment of a Dream, p. 1166.
11The Shuttle Tile Story, pp. 2427;
The Challenging Scale of the Bird, pp. 409410;
Space Shuttle: Fulfillment of a Dream, pp. 11601163.
12The Challenging Scale of the Bird,
pp. 403413; NASA Dryden Press Release, (no title), 18 January
1980.
13The Challenging Scale of the Bird,
pp. 403413.
Updated
April 5, 2001
Bill Barry, NASA Chief Historian
Steve Garber, NASA History Web Curator
For further information, e-mail histinfo@hq.nasa.gov
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